lockie
Active Member
- Joined
- Feb 12, 2017
- Messages
- 70
- Country Flag
well let me start by saying, what i did this weekend was (what i thought) slightly beyond my mechanical knowledge. So you may have to excuse me... i might not be calling certain parts by the right name.
And why was i removing the head you might ask.... for the past 4-5 weeks i've noticed that the radiator was over pressurising and pushing all the coolant out the overflow, and on two occasions it started to get a bit hot.
Saturday about 10:30 is when i kicked off, in that day i got everything off that was in the way - fuel lines injectors, rocker cover, timing belt etc.....
Injector 6 had a little bit of green/white crystals building up on it. Not a good sign, all the others however didn't look too bad...
That took my brother and me a couple of hours (over a few beers, and we definitely weren't rushing)
along with a shit load of pictures.
Sunday was the big day (i didn't realise how much i had left to do) i thought i was going to be gone by early afternoon.... wrong! I left at 7pm.
We took off the turbo, the dump pipe, outlet manifold, camshaft and finally the head!
Unfortunately upon inspection i found that piston no 6 had a nasty little surprise on it (all the pictures should be attached below)
So now i'm having the head sent off to get crack tested tomorrow and then i guess ill see if its possible to replace just one piston, try and save myself the cost of a full rebuild (i'm only an apprentice so im not exactly rolling in it)

And why was i removing the head you might ask.... for the past 4-5 weeks i've noticed that the radiator was over pressurising and pushing all the coolant out the overflow, and on two occasions it started to get a bit hot.
Saturday about 10:30 is when i kicked off, in that day i got everything off that was in the way - fuel lines injectors, rocker cover, timing belt etc.....
Injector 6 had a little bit of green/white crystals building up on it. Not a good sign, all the others however didn't look too bad...
That took my brother and me a couple of hours (over a few beers, and we definitely weren't rushing)
along with a shit load of pictures.
Sunday was the big day (i didn't realise how much i had left to do) i thought i was going to be gone by early afternoon.... wrong! I left at 7pm.
We took off the turbo, the dump pipe, outlet manifold, camshaft and finally the head!
Unfortunately upon inspection i found that piston no 6 had a nasty little surprise on it (all the pictures should be attached below)
So now i'm having the head sent off to get crack tested tomorrow and then i guess ill see if its possible to replace just one piston, try and save myself the cost of a full rebuild (i'm only an apprentice so im not exactly rolling in it)
















